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Best time as of 4-7-05: 6.90
@ 102
10
pounds of boost made 565 HP 632 rwtq pump gas
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here to email Jonathan
Current Combo:
Turbo
System:
HP Performance stage 1 turbo kit
T-60 turbo
Engine and Management System:
Probe Forged 347 Stroker
Stock block (studded and girdled)
X cam
Stock ECU, Autologic dynotune
Induction and Fuel:
Custom Fabricated upper with stage 3 ported lower
Victor Jr. Heads (out of the box)
Complete Aeromotive System (tank to rails)
60 lb Siemens Deka Injectors
Ignition and Exhaust:
MSD Digital 6
Blaster coil
10.4 Taylor wires
3.5 down pipe
Custom y pipe (3 inch)
Borla Mufflers strait through design (3 inch)
Tranny and rear:
Tremec TKO II
Spec 3 clutch
Aluminum Driveshaft
3.55 gears and 31 spline Moser Axles
Ected differential with c-clip elims
Front Suspension:
Lakewood 90/10
Eibach Drag Launch Springs
Steeda CC Plates
Rear Suspension:
Lakewood 50/50
Eibach Drag Launch Springs
HPM Mega Bit Jr’s
Steeda upper control arms
HPM Sub frames and driveshaft loop
Competition Engineering anti-roll bar
Tires and rims:
17” Stock 93 Cobra wheels (welds on the
way)
245 kumho (front)
255 Nitto NT555 (rear)
Track: Weld 15x3.5 with front runners
Weld 15 x 8 with ET Street Radials 275/50/15
Body:
Stock
Future plans:
Build
a 4 bolt block this winter and upgrade my ECU.
Also I am going to upgrade to T-66 or T-76 turbo
Background:
When I bought
the car it was in bone stock form, with a Paxton SN-92. This car with street
tires would run 8.90's in the eight mile. From this point I decided to change
a couple of things, to up the power level. I decided to change the cam and
Intake. This would turn out to be a disaster. I paid a guy to install the
cam and intake, but when he was scraping off the gasket from the timing chain
cover, some fell into the oil pan. I arrived to pick up the car and take it
for a test drive and I did not get a mile and the motor started knocking!!
I looked down and I had no oil pressure. I had the car towed home trying
to minimize the damage that had occurred to the bottom end of the motor. The
next weekend I tore the motor down and was able to scrape a handful for blue
timing cover gasket off of the oil pickup. Spun all but one bearing. From
this point I decided if I wanted something done right, I better do it myself.
The car sat for a couple of months while I was deciding how I wanted to fix
the car. I decided to build a 347. Drew Davis from Rotating Dynamic was called
on to build the motor. After about 5 months I had the motor back in the car
and ready to take it back to the drag strip. During
the down time, I upgrade most of the suspension and ignition system. My first
run down the drag strip on Nitto drag tires I run a 7.90 @ 83 mph. A couple
months past and I took the car down to Rockingham dragway in North Carolina
and ended up running a best of 12.10 @ 116 with a 1.8 60 foot time.
Once winter came back around,
I decide to sell the SN-92 and actual put the boost friendly pistons to work.
I installed a Kenne Bell Blowzilla with a 12 pound pulley. I will not lie,
I was amazed by the torque and power that this supercharger generated but
with most superchargers I ran into detonation issues and would never get the
Kenne Bell to run like it was supposed too. So off came the KB. I call HP
performance and talked with there staff and they put me into a stage1 turbo
kit. I got this turbo right before everyone started ordering them, so it only
took about 2 months for me to receive the kit. I installed the kit and had
the exhaust reworked. I can not describe how much more power I had with the
turbo and that was with 8 pounds of boost!! With no tuning I took the car
to the local 8th mile drag strip. I did not plan to drag the car but I got
persuaded to make a pass. I had my street tires on at the time. I left the
line easy and got into it, it spun through 1st, second and finally caught
traction n third gear. I ended up running an 8.30 @ 102 mph.
I know I was generating a good
amount of power and decided it was time to take the car and get it dyno tuned.
I called up Randy Haywood @ Haywood Speed shop and he was eager to start tuning.
I pulled the car on the Dyno and made the first pull. With no tuning, not
even a chip in the car, the car made 565 Hp and 632 TRQ @ 4200 RPM's. I was
amazed and then pissed because the reason Randy had stopped the pull was due
to me running out of Fuel. So I drove the car 2 hours back home and let the
car sit until I could gather enough money to upgrade my fuel system. I bought
a complete Aeromotive Kit and 60 pound injectors. I once again drove the car
back down to Haywood Speed shop to finish the Tune. This time the car would
take about 17 pulls to get it right. To save the stock Block, we de-tuned
the car and locked out the total timing @ 18 degrees. Showing 8 PSI and 18
degrees of total timing, the car made 542 HP and 610 TRQ. I was happy with
that and drove the car home. Since that time I have made a couple trips to
the drag strip, the best time I have ran is a 6.90 @102 with a 1.59 60 foot.
I will never own another belt driven power adder again!!! Thanks for the opportunity
to be featured on such a great website.
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